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Roger's RRC: An update

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TwoSheds
Posts: 1092
Joined: Thu Jan 18, 2007 8:01 pm
Location: M1/M62
Full Name: Roger Watkinson

BUGGER!

Postby TwoSheds » Thu Sep 16, 2010 9:07 am

After several months trouble free motoring I have just gone out and noticed a fairly bad steering box leak from there the steering shaft goes in. Good timing eh?
Only thing changed is that I have parked with the steering on full lock, clutching at straws I know, but I am hoping that this has caused what was a very minor weep to turn into a full on leak. Maybe it will be ok when pointing forward... Hmm - I can see that straw floating away as I speak.

I am going to stock up on drybollick fluid and come tomorrow anyway... Hopefully it won't get any worse.

ten minutes later: It's not as bad as I thought - possibly leaking from the big round front 'plate' although difficult to tell since it gets whipped around. Anyway, the level is only a little bit down so I am more optimistic now...

kingsonlim
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Joined: Tue Jun 05, 2007 4:06 pm
Location: Sherburn in Elmet
Full Name: Kingson Lim

Postby kingsonlim » Thu Sep 16, 2010 11:45 am

try adding a cap full of brake fluid. That'll swell the seals a little and stop the leak. Worked on mine. Am waiting for my replacement ox to arrive.

TwoSheds
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Joined: Thu Jan 18, 2007 8:01 pm
Location: M1/M62
Full Name: Roger Watkinson

Postby TwoSheds » Thu Sep 16, 2010 12:36 pm

kingsonlim wrote:try adding a cap full of brake fluid. That'll swell the seals a little and stop the leak. Worked on mine. Am waiting for my replacement ox to arrive.

ox?

TwoSheds
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Joined: Thu Jan 18, 2007 8:01 pm
Location: M1/M62
Full Name: Roger Watkinson

Postby TwoSheds » Thu Sep 16, 2010 2:32 pm

I am hopeful that it is ok. I think that the fluid had gathered on the chassis rail when parked slightly up hill and that turning it around had released it - if that's the case then the amount on the ground (perhaps a tablespoon full) has come out over several weeks. A couple of hours ago I wiped it all off and went for a ten mile 50mph drive and only a small amount of leakage is evident (not enough to drip yet)
Fingers crossed!

TwoSheds
Posts: 1092
Joined: Thu Jan 18, 2007 8:01 pm
Location: M1/M62
Full Name: Roger Watkinson

Dartmoor!

Postby TwoSheds » Tue Nov 02, 2010 6:18 am

Well, we made it to and from Dartmoor and even managed to find a ford and do a bit of offroading as well... Never skipped a beat :D

Image

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tecnick
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Joined: Tue Jan 09, 2007 9:52 am
Location: Leeds
Full Name: Nick Adams

Postby tecnick » Tue Nov 02, 2010 8:02 am

V8 to dartmoor, hope the bankmanager is in a good mood, would it have been cheeper to get the train and buy a smoking deisel when you got there :?:

Just being silly again, looks like you had a good time.

Cheers Nick
If it ain't broke, I'd be bloody suprised.

TwoSheds
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Joined: Thu Jan 18, 2007 8:01 pm
Location: M1/M62
Full Name: Roger Watkinson

Postby TwoSheds » Tue Nov 02, 2010 8:31 am

Had a GREAT time thanks :)

660 miles, 220 litres of gas costing £135 - roughly equivalent to 28mpg at diesel prices (if my maths is ok)... I am ok with that - especially since I can claim it back :D :)

Roger

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tecnick
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Location: Leeds
Full Name: Nick Adams

Postby tecnick » Tue Nov 02, 2010 1:15 pm

Not bad at all, good stuff, and its less sooty.

Cheers Nick
If it ain't broke, I'd be bloody suprised.

TwoSheds
Posts: 1092
Joined: Thu Jan 18, 2007 8:01 pm
Location: M1/M62
Full Name: Roger Watkinson

C-C-C-COLD!!!

Postby TwoSheds » Wed Dec 22, 2010 10:43 am

Even with the fabled V8's ability to produce excess heat, I have been feeling the cold a bit recently in the RRC, so I decided to insulate it. I used two camping-mats and some double-sided tape, and after 5 miles it's like a sauna!
A lot quieter too :)
I got the mats from that Class Ollsen (or whatever it is) in Leeds - 14mm thick and less than £6 each, not bad I think...

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tecnick
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Full Name: Nick Adams

Postby tecnick » Thu Dec 23, 2010 8:58 am

My wife came back from christmas shopping with loads of stuff from that shop, must pay it a visit one day, I have only got as far as 4plus4 for years, dont much like the city.

Nick
If it ain't broke, I'd be bloody suprised.

kingsonlim
Posts: 422
Joined: Tue Jun 05, 2007 4:06 pm
Location: Sherburn in Elmet
Full Name: Kingson Lim

Postby kingsonlim » Thu Dec 23, 2010 7:43 pm

bought a rechargeable work light (60 led) there for 6.98....good deal I think..!!

TwoSheds
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Location: M1/M62
Full Name: Roger Watkinson

LPG and all that. Warning: Long and boring post!

Postby TwoSheds » Sat Jan 08, 2011 11:01 am

I have had a go (again) at tuning my car since - although it seemed to run ok - it had something of a reluctance to accept large throttle openings at medium revs. For example on the M6 at 55mph I would have to change down to 4th to hold my speed on the climb up to Saddleworth when returning from the Dark Side.

Firstly I decided to check out exactly how it was going with a few tests:
At low revs, any throttle setting was fine: It ran smooth and pulled well.
At medium revs on a small throttle - it was also fine, but at medium revs on a medium (or higher) throttle it was flat: i.e it didn't want to pick up, the more you open the throttle the flatter it seemed.
Interestingly, at high revs any throttle setting was fine: Once past 3500 rpm it pulled really well :)

My first thought then was timing. Since fitting MegaJolt I had never had a serious go at optimising it since right out of the box with my guestimated maps, it worked pretty well. And anyway- without a rolling road the differences that small changes make are really hard to detect. So a couple of days were spent in a cycle of web-searching, changing the map, and road testing. A lot of frustration ensued as I just couldn't get rid of the flat-spot. After two days I was pretty certain that timing wasn't the cause of the flat-spot. Not saying that the timing is right, mind - just that it's not the cause of the flat spot.

So I started looking at the LPG setup...

My car has the most basic setup you can get - a vapouriser, a manual power-valve and an annular mixer. According to the internet, there should be three adjustments available:

Idle bleed screw: a simple needle valve that allows an amount of gas to bleed into the system continuously - this is to compensate for there being virtually no vacuum at the mixer at tickover and does not pass enough gas to enough to effect anything else. It is quite common (depending on physical variations in setup) for this to be entirely closed. This looks like an old carburettor mixture screw and sits on the side of the vapouriser.

Bias control screw: This controls the amount of spring pressure holding the main gas feed valve (in the vapouriser) closed against the force generated on the diaphragm by the mixer vacuum. The more this is screwed in the more vacuum it takes to open the valve and get gas. It is a hex-headed bolt set near the idle bleed screw.

Power valve: A simple valve which progressively blocks off the pipe which feeds the gas from the vapouriser to the mixer. It obviously effects how much of the vacuum at the mixer is 'seen' by the vapouriser.

Having got this straight I then started looking for instructions on setting up an open loop system.

First point is that you really need some sort of exhaust gas analyser, and preferably one that could be used while driving so that you can check various engine loadings. Now I had already gone part way towards this last summer when I installed a lambda sensor and constructed a small indicator circuit - however it appeared at the time that the circuit did not work correctly, so assuming I had got it wrong (it was my own design) I abandoned it. Anyway, now my thoughts turned to it and the possibility of either getting it working or at least of savaging some bits, so I located it (under the settee!!! ???) and set-to testing it again. Guess what? It works! It always did. All that was wrong was the setting of one of the trimmers... D'OH!

So I wired the display to the lambda and started it up. Setting the display unit up proved troublesome - I didn't have a reference voltage and I didn't know what the mixture currently was, so what I ended up doing was running it on petrol and setting the trimmer so that the indicator would go from rich to lean under various conditions. Still not sure how close it is but at least I now have a rich-lean indicator.

Now for the gas. Always lean. That's it - always lean. Tried the power valve all over the place - always lean. Tried the idle bleed all over - always lean.

I couldn't try the bias valve because my unit didn't have one. But wait-a-mo... From my new found understanding (?) of the workings of the vapouriser - it HAD to have one. A good root-around with a mirror and torch found nothing like the pictures, but in the place where I had expected it to be (remember it should be a 10mm hex-head adjuster sticking out the side) I found what looked like a counter-bored hole with an allen bolt sunk well down. I had seen this before, but since it was tight down I had assumed it was a fastener and not an adjuster - but with my new-found knowledge of the internals of the vapouriser - I realise that I was wrong. I gave it a bit of welly and it came loose, and a couple of runs in and out freed it up to the point where it now felt like an adjuster. A quick try with the engine running show that it definitely has an effect.

So now I had all three adjusters available and some basic understanding of what they do, and a working exhaust gas analyser.

Here comes the science bit:
An engine at a given revs consumes a given amount of air.
Twice the revs requires (more or less) twice the air.
The amount of air directly effects the velocity of the air through the mixer.
According to O-level physics, Bernoulli's equation shows that (within limits) the pressure in the venturi will be inversely proportional to the square of the velocity.
So the vacuum produced by the venturi (mixer) in the gas supply pipe is proportional the the square of the revs.
The amount of gas supplied by the vapouriser is roughly proportional to the vacuum that it sees from the engine.

From the above we can see that without the 'power-valve' the mixture would go horribly rich at the higher end of the revs. The power-valve is also subject to Bernoulli's equation, but works in opposition to the venturi and so tends to make the amount of gas supplied more linear with regard to the amount of air being drawn into the engine.

So - it now becomes clear that the idle screw can be forgotten about until everything else is done, the bias valve adjusts the mixture across the range, and the power-valve compensates for the non-linearity of the mixer.

I warmed the engine thoroughly and set to:

Since my gauge was showing lean at all times on gas I started by screwing out the bias adjuster. Unfortunately it just stayed weak and after a few turns it actually started to run rough.. So I set it as rich as I could and went for a test-drive. The only way I could get a rich indication was right at the top of the revs (5000rpm plus) on a wide open throttle. Previously I had not been able to get a rich indication at all on gas so this was actually an improvement!

Two days of screaming back and forth around local roads and adjustments in lay-bys later and I have only improved a little on this position: At tickover the mixture wobbles around lean-rich-lean. When driving, under all conditions except flat out at high revs it shows lean.

The effect on performance has been dramatic though - especially in the 2000-3500rpm range where it now pulls really quite well (although remember that I have not driven any other V8s so I don't really have a 'control' sample).

So finally - why am I unable to get the mixture right throughout the range? Well I suspect that the vapouriser is a little the worse for wear. I think that the non-standard bias adjuster may be leaking air into the system when screwed out which might explain why I can't get it to go fully rich and I am not sure what the rest of the internals are like. I have drained the 'heavy-ends', but cannot fully service the unit without a gasket set which would cost £25, and with a new unit costing less that £70 and the fact that mine has obviously been bodged (the allen bolt), I have decided that once the Christmas spending has worked it's way through, I will replace it. I am also hanging my nose over a Blos LPG carburettor - which replaces the mixer with a vacuum-controlled variable choke system (like an SU carburettor) which removes the need for the power-valve, but that may have to wait a while since there are many other things I need to sort first.

For now though, it is running a LOT better than it was and (hopefully) will be rather more economic than it has been.

If anyone is still reading - thanks! Hope you enjoyed it ;)

Roger

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Bo
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Full Name: Scot Chegg

Postby Bo » Sat Jan 08, 2011 2:29 pm

Hi Roger, are you certain you have no leaks in the inlet manifold as they are notorious for not sealing? Which valley gasket are you using, tin or composite?
5/4 of people admit that they’re bad with fractions.

TwoSheds
Posts: 1092
Joined: Thu Jan 18, 2007 8:01 pm
Location: M1/M62
Full Name: Roger Watkinson

Postby TwoSheds » Sat Jan 08, 2011 3:16 pm

Bo wrote:Hi Roger, are you certain you have no leaks in the inlet manifold as they are notorious for not sealing? Which valley gasket are you using, tin or composite?
Good point - it's a tin gasket with some rust in the valley, but all the plugs look the same (I would have expected them to be uneven if there was an inlet manifold leak?) and it doesn't seem (to me) to have any other 'intake leak' type of problems. I will try having a squirt around with some cold-start as a check though and at less than £20 I think I will change it anyway when I next do any engine work..
Thanks for the tip.

Roger

PS: As an aside, the point at which I decided that the vapouriser was the problem was when I found that unscrewing the bias adjuster didn't seem to be working after a couple of turns (it got worse in fact). From what I have read I should be able to screw this out to the point where gas is being supplied under positive pressure which should result in it being horribly rich - whereas at the point where the engine started to run rough it was still showing lean. I can, however, get it to go rich at tickover by using the idle mixture screw.

LATER:
Checked all around with a can of cold-start (legacy from my Disco days) but no leaks evident, although the car did catch fire while I was doing it :o
Not as a result of the testing you understand - I had the door open and the puddle light shorted and started burning. Luckily I have quick release battery leads but even so, by the time I had disconnected the battery and got the bottom of the door card opened up there were significant flames in there! I can now vouch for the fact that snow is a good extinguishant :)

TwoSheds
Posts: 1092
Joined: Thu Jan 18, 2007 8:01 pm
Location: M1/M62
Full Name: Roger Watkinson

Postby TwoSheds » Mon Jan 31, 2011 8:08 am

A bit more fiddling and I have this at tickover:

http://www.youtube.com/watch?v=MFnfT_0UoII

But still can't get it to run anything but lean while driving, although checking the plugs after a motorway run indicates that it is not that lean...


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